Re: [問題]空中的速度..跟地面的速度..有不同嗎?
※ 引述《svuper (mika)》之銘言:
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: 之前有看過網路上的文章,剛剛搜尋了一下
: 這架747-sp在空中,4號發動機在2月15到2月19的4天中
: 發動機總共熄火了3次
: 2/15 在FL410熄火 降到FL300重新啟動
: 2/18 在FL430熄火 降到FL280重新啟動
: 2/19 在FL410熄火 失控掉到9000ft
: 所以高度一掉就是3萬2千英尺 = =
: 飛機機尾的水平安定面左右都斷了一部份
: 我想如果是我可能在機上嚇到失禁了吧0rz
以下摘錄自NTSB調查報告,嚴格來說NTSB並不認為發生事故當天四號發動機是熄火
3.1 Finding
1. The flightcrew was properly certificated and qualified.
2. The Changing airspeeds encountered by Flight 006 and the resultant
compensating throttle adjustments were caused by wind speed variations.
3. The No.4 engine did not flame out, but "hung" at about 1.0 EPR.
4. During his attempt to recover the No.4 engine, the flight engineer did
not close the bleed air valve switch before advancing the No. 4 throttle.
5. The other three engines did not lose thrust nor did they flame out.
6. The captain did not disengage the autopilot in a timely manner after
thrust was lost on the No.4 engine. The autopilot effectively masked
the approaching onset of the loss of the airplane.
7. The captain was distracted from his flight monitoring duties by his
participation with the flight engineer in the evaluation of the No.4
engine's malfunction.
8. With the exception of the loss of thrust on the No.4 engine, no other
airplane malfunction affcted the performance of the airplane; the loss
of thrust on the No.4 engine did not contribute to the accident.
9. The captain was also distracted by his attempts to arrest the airplane's
decreasing airspeed, and this also contributed to his failure to detect the
airplane's increasing bank angle.
10. The lateral control deflections required to maintain level flight under
conditions of thrust asymmetry and decreasing airspeed exceeded the
limits of the autopilot's lateral control authority, causing the airplane to
roll and yaw to the right. The captain lost control of the airplane when,
after disengaging the autopilot, he failed to make the proper flight control
corrections to recover the airplane.
11. The damage to the airplane was a result of the acceleration forces and
high airspeeds that occured during the upset and recovery maneuvers.
3.2 Probable Cause
The National Transportation Safety Board determines that the probable cause
of this accident was the captain's preoccupation with an inflight malfunction
and his failure to monitor properly the airplane's flight instruments which
resulted in his losing control of the airplane.
Contributing to the accident was the captain's over-reliance on the autopilot
after the loss of thrust on the No.4 engine.
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◆ From: 71.237.67.217
※ 編輯: kaichun1216 來自: 71.237.67.217 (01/09 23:58)
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